Indexed by:
Abstract:
A large-scale shaking table test for subway station structure built in the liquefiable saturated fine sand soil is implemented. Partial test results are analyzed in this paper. The acceleration time-histories and the dynamic pore water pressure ratio time-histories of ground soils are given. During the whole process of testing, it is obvious that the soils at the top of model ground and beside the subway station structure is liquefied firstly. Then the soil far from the subway station structure and at the bottom of model ground is liquefied with the increasing of the peak value of acceleration inputted by the surface of shaking table. However, the soils under the subway station structure is not liquefied during the whole process of testing. At the same time, the subway station structure uplifts badly during the soil liquefaction.
Keyword:
Reprint Author's Address:
Email:
Source :
Journal of Earthquake Engineering and Engineering Vibration
ISSN: 1000-1301
Year: 2007
Issue: 3
Volume: 27
Page: 163-170
Cited Count:
WoS CC Cited Count: 0
SCOPUS Cited Count:
ESI Highly Cited Papers on the List: 0 Unfold All
WanFang Cited Count:
Chinese Cited Count:
30 Days PV: 5